Title: University Of Vermont Central Plant Control Systems Upgrade
1University Of VermontCentral Plant Control
Systems Upgrade
- Sal Chiarelli
- Director of Physical Plant
- Michael Wells
- Central Plant Supervisor
- Ray Racine
- Senior Controls Engineer Hallam-ICS
2Utilities Master Plan Main Schemes
- Document existing conditions
- Develop central chilled water plant
- Upgrade steam distribution system
- Minimize single point failure points
- Eliminate choke points on the distribution system
- Retire old inefficient equipment
- Upgrade Building Control Systems
- Co-generation possibilities
- Central chilled water plant
- Capacities/limitations
- Utility Corridors/ Plan the campus
- Reduce demand (all utilities)
- Spend now to save later/reduce excavation
- Upgrade Central Plant Control Systems
3Westinghouse to DeltaV
- From the old to the New
- From Charts that required Nightly changing
- Felt tip pens
- Ink cartridges
4The Amazing Conversion
- New Air Conditioning
- Upgraded Electrical Distribution
- New High Efficiency Lighting
- New Computer Terminals
- New Office Furniture
- Air Filtration System
- Increased Square Footage of Room
- Installed State-of-the-Art Delta-V Operating
System
5The Beginning of New
- The installation of the new Delta-V Controllers
- New Air Conditioning to maintain constant
temperature to assure life expectancy and
computer function
6Each New Components Benefits
- New Air Conditioning
- Allows for higher quality air supply
- Computers have a safe environment
- Computers operate optimally
- Employees have a comfortable safer work
environment which increases moral and
productivity
7Each New Components Benefits
- Upgraded Electrical Distribution
- Allowed for more efficient VFDs to be installed
thus decreasing electrical demands - Decreased the possibility of single point
failures - Made maintenance of the system more user friendly
- Centralized three panels
- Afforded the opportunity for further expansion
8Each New Components Benefits
- Computerization of Control System
- Allowed for more efficient Reading to be Compiled
- Decreased the possibility of single point
failures - Made maintenance of the system more user friendly
- Centralized Control of the five Boilers
- Afforded the opportunity for further expansion
9Each New Components Benefits
- Computerization of Control System
- Allowing for custom Alarming on the new computer
System - A better view of Plant Systems
10Making way for the New
- First Panels To be removed were s 1 2
- Boiler Controls that were installed in 1970
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11The Old BMS Control Panels
- Not only the Pneumatics were being removed but
the old Burner Management System was going to be
Computerized
12All of This Turned Into..
13THIS!!!!!!!!!!
14Halfway There
15Delta-V The Life Line of Campus
16Delta-V Hallam-ICS
- UVM selected the technicians of Hallam-ICS to
- Install Calibrate Instruments
- Work with Programmer to start-up boilers
- Initial Controls Vendor Programmer did not have
DeltaV experience - Code was not clean or consistent
- Start-up went poorly
- Operation of Boilers unreliable
- Trips not recorded
- UVM did not trust DeltaV system
17UVM forges a partnership
- Technicians told Mike about their programmer with
boiler experience - UVM contracted programmer for some simple fixes,
which were successful built trust - Programmer had boiler experience on several
platforms, but had never touched DeltaV - Hallam-ICS had already committed to learning this
system now a real world chance - UVM agreed to let programmer learn on-line for 1
week (Hallam-ICS expense) - Programmer attended custom 2-day training by
Emerson (Hallam-ICS expense)
18DeltaV Gets a Facelift
- UVM contracts Hallam-ICS to convert Boiler 1
- New System New Rules
- Work with Operators to set color standards
- Work with burner vendor to customize (from
scratch) BMS code to these burners - NFPA is only
part of BMS - Rewrite (from scratch) Combustion Controls to
give reliable and efficient cross-limiting
(understand burner efficiency Stoichiometry) - Design Graphics for easy understanding and simple
command entry - Start / Stop Auto / Manual Setpoints
- Accurate First Out reporting
- Sensible Alarm strategies (color, sound,
flashing) - Custom Reports from Historical Trends Events
19Simple Graphics
20Simple Graphics
21Simple Graphics
22Simple Graphics
23Meaningful Help Always Available
24Meaningful Help Always Available
25DeltaV Redeemed
- Boiler 1 Started-Up on New Controls
- One Day Start-Up for Combustion BMS
- Next 3 Boilers in 2 days Boiler 5 / 2 days
- Boiler House Trusted the System
- Operators liked new interfaces
- Adopted Pop-Up for Controls Philosophy
- Screen Colors match piping colors in field
- Alarm and Warning set at sensible levels
- BMS Christmas Tree provides troubleshooting for
light-off issues - Standard Screen Navigation for all displays
- Overviews for system status
26Conversions are Never Finished
- Winter Loads show gradual changes
- Summer was not as forgiving
- Two Steam Absorption Chillers came on-line
- Wanted 20 KPPH Steam Right Now!!
- Plant Master could not respond without
occasionally dumping a boiler - Three days of work to re-tune Plant Master
- Re-Test for winter loads in December
27Just one More Thing
- Then came the Central Cooling Plant
- Two Steam Driven Chillers
- Four Towers and Fans
- Pumps Drives
- Comm. Interface to Chillers (Modbus Serial)
- Provide summer Load to Boiler House
- Used existing Control Philosophy
- Upgrade successfully integrated into DeltaV
28More Equipment
29Running Systems
30UVM Central Utilities Success Formula
- Consider current and Future Needs
- Develop Standards and stick with them
- Develop Equipment Vendor Relationships and
Technical Support Relationships - Keep it Simple
- Meet code requirements
- Make it as efficient as possible
- Dont make it any more complicated than
absolutely necessary - Train your whole Team to run the system