Title: Terumo Cardiovascular Systems: Oxygenator Production Improvement
1Terumo Cardiovascular SystemsOxygenator
Production Improvement
- University of Delawares Senior Design Team
- Tom Craig
- Mike Giuliano
- Ronit Lilu
- Chase Ross
- Kate Staley
2Description of Project
- Project Goals
- Improve the efficiency of Reservoir Assembly
production line via reduction in downtime, change
over time, and cycle time. - Employ lean manufacturing techniques from the
ground up such as participation in a Kaizen event
3Assembly Line
Reservoir Inspection
Lid Assembly
VR Station
CR Station
Leak Tester
VR
CR
Lid
Final Assembly
Lid Line
Jig
4Current Floor Layout vs. Future Floor Layout
Reservoir Assembly Table
CR
VR
Lid Line Assembly Table
Product Flow
5Lean Manufacturing Techniques
- The Kaizen event
- Attended a meeting with representation from
operators, manufacturing, production supervisors,
engineering, and plant leadership to discuss
improvements - Time study
- Spaghetti diagrams
- Value Stream Mapping (VSM)
- Value Added, Non-Value Added Time
6Customers Wants
- Customers Terumo Management, Terumos Floor
Staff, Surgeons, Hospitals, Patients
7Metrics and Target Values
8Current Floor Layout vs. Future Floor Layout
Product Flow
Reservoir Assembly Table
1 Pass of 3 Steps
6 Passes of 3 Steps Each
CR
VR
Lid Line Assembly Table
- VR walking distance/day 6.6 miles
- CR walking distance/day 1.5 miles
- VR walking distance/day .5 miles
- CR walking distance/day 0.3 miles
9VR Current State vs. Future
Time Saved mostly due to table redesign and
offline production Walking Time - 6.3 seconds
10VR Concepts
- Rotate lid assembly table and align it with
Chemical Table - Redesign Chemical Table and L it with the
assembly line - Design and manufacture additional jig
- Take wings off jigs on table
- Sensors on bins to force order
11CR Current State vs. Future State
Time Saved 9.9 seconds reduced time through
elimination of walking (moving caps) and addition
of the chemical sensor. Note Increased VA time
due to addition of inspection tasks
12CR Concepts
- Move caps down to reservoir inspection
- Time sensor for chemical dipping
- Move CR cart closer to operator
- Increase inspection duties
13Reservoir Inspection Current State vs. Future
State
Reduction in Inspection Duties Line Balancing
Additional responsibilities (placement of 6 more
caps)
14Proposed Floor Layout
Table at VR Station
Table at CR Station
15Final VR Table
Tricots
Drainage cages
Fume hood
Small tubes
Large tubes
Jig
Position forcing tray
16Preparation before Implementing
- Risk Analysis
- Met with a team of Terumo associates including
engineering, upper management, quality manager,
and manufacturing associates to assess risk via a
Terumo Risk Analysis template. - Given GREEN light to go ahead
- Update Standard Operating Procedures
- Drafted changes to the SOP via text and pictures
which was then reviewed and approved by Terumo
17Implementation/Testing
- Off-line implementation
- Operator at Terumo tested the new set-up of VR
table on manufacturing floor to make sure
everything easy to reach and functions well.
18Implementation/Testing
- Parts were loaded into bins to test how much they
hold. - Improvements
- Tricot and drainage cage bin sizes increased to
increase capacity - Positioning adjustments made
19Performance Metrics
20Path Forward
- Terumo will manufacture the new bins for the
increased capacity and new arrangement. - Design can then be implemented on the line.
- Additional time studies and spaghetti diagrams
are recommended once implemented on the line. - Sensors will be implemented at a later date by
Terumo.
21Project Cost
Note Terumo will use their own Machine Shop to
manufacture the jig and VR Chemical Hood. Team
will use UD Machine Shop to manufacture bins.
22Revenue Analysis
- 15 additional units/hour
- 30,960 additional units/year
- 12,384,000 additional revenue/year
- 1,145,520 additional material cost/year
- 11,238,480 net gain/year
23Project Summary
- Lean manufacturing techniques such as VSM used to
increase efficiency of manufacturing process - Improved ergonomics for operators
- Maximized space used
- Decreased cycle time
- 11.2 million net gain/year
24Questions?