Terumo Cardiovascular Systems: Oxygenator Production Improvement - PowerPoint PPT Presentation

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Terumo Cardiovascular Systems: Oxygenator Production Improvement

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Title: Terumo Cardiovascular Systems: Oxygenator Production Improvement


1
Terumo Cardiovascular SystemsOxygenator
Production Improvement
  • University of Delawares Senior Design Team
  • Tom Craig
  • Mike Giuliano
  • Ronit Lilu
  • Chase Ross
  • Kate Staley

2
Description of Project
  • Project Goals
  • Improve the efficiency of Reservoir Assembly
    production line via reduction in downtime, change
    over time, and cycle time.
  • Employ lean manufacturing techniques from the
    ground up such as participation in a Kaizen event

3
Assembly Line
Reservoir Inspection
Lid Assembly
VR Station
CR Station
Leak Tester
VR
CR
Lid
Final Assembly
Lid Line
Jig
4
Current Floor Layout vs. Future Floor Layout
Reservoir Assembly Table
CR
VR
Lid Line Assembly Table
Product Flow
5
Lean Manufacturing Techniques
  • The Kaizen event
  • Attended a meeting with representation from
    operators, manufacturing, production supervisors,
    engineering, and plant leadership to discuss
    improvements
  • Time study
  • Spaghetti diagrams
  • Value Stream Mapping (VSM)
  • Value Added, Non-Value Added Time

6
Customers Wants
  • Customers Terumo Management, Terumos Floor
    Staff, Surgeons, Hospitals, Patients

7
Metrics and Target Values
8
Current Floor Layout vs. Future Floor Layout
Product Flow
Reservoir Assembly Table
1 Pass of 3 Steps
6 Passes of 3 Steps Each
CR
VR
Lid Line Assembly Table
  • VR walking distance/day 6.6 miles
  • CR walking distance/day 1.5 miles
  • VR walking distance/day .5 miles
  • CR walking distance/day 0.3 miles

9
VR Current State vs. Future
  • Current State
  • Future State

Time Saved mostly due to table redesign and
offline production Walking Time - 6.3 seconds
10
VR Concepts
  • Rotate lid assembly table and align it with
    Chemical Table
  • Redesign Chemical Table and L it with the
    assembly line
  • Design and manufacture additional jig
  • Take wings off jigs on table
  • Sensors on bins to force order

11
CR Current State vs. Future State
  • Current State
  • Future State

Time Saved 9.9 seconds reduced time through
elimination of walking (moving caps) and addition
of the chemical sensor. Note Increased VA time
due to addition of inspection tasks
12
CR Concepts
  • Move caps down to reservoir inspection
  • Time sensor for chemical dipping
  • Move CR cart closer to operator
  • Increase inspection duties

13
Reservoir Inspection Current State vs. Future
State
  • Current State
  • Future State

Reduction in Inspection Duties Line Balancing
Additional responsibilities (placement of 6 more
caps)
14
Proposed Floor Layout
Table at VR Station
Table at CR Station
15
Final VR Table
Tricots
Drainage cages
Fume hood
Small tubes
Large tubes
Jig
Position forcing tray
16
Preparation before Implementing
  • Risk Analysis
  • Met with a team of Terumo associates including
    engineering, upper management, quality manager,
    and manufacturing associates to assess risk via a
    Terumo Risk Analysis template.
  • Given GREEN light to go ahead
  • Update Standard Operating Procedures
  • Drafted changes to the SOP via text and pictures
    which was then reviewed and approved by Terumo

17
Implementation/Testing
  • Off-line implementation
  • Operator at Terumo tested the new set-up of VR
    table on manufacturing floor to make sure
    everything easy to reach and functions well.

18
Implementation/Testing
  • Parts were loaded into bins to test how much they
    hold.
  • Improvements
  • Tricot and drainage cage bin sizes increased to
    increase capacity
  • Positioning adjustments made

19
Performance Metrics
20
Path Forward
  • Terumo will manufacture the new bins for the
    increased capacity and new arrangement.
  • Design can then be implemented on the line.
  • Additional time studies and spaghetti diagrams
    are recommended once implemented on the line.
  • Sensors will be implemented at a later date by
    Terumo.

21
Project Cost
Note Terumo will use their own Machine Shop to
manufacture the jig and VR Chemical Hood. Team
will use UD Machine Shop to manufacture bins.
22
Revenue Analysis
  • 15 additional units/hour
  • 30,960 additional units/year
  • 12,384,000 additional revenue/year
  • 1,145,520 additional material cost/year
  • 11,238,480 net gain/year

23
Project Summary
  • Lean manufacturing techniques such as VSM used to
    increase efficiency of manufacturing process
  • Improved ergonomics for operators
  • Maximized space used
  • Decreased cycle time
  • 11.2 million net gain/year

24
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