Title: Clear Fiber Cable Light Tightening
1 Clear Fiber Cable Light Tightening
- Howard Budd
- University of Rochester
- MINERnA PMG Meeting
- Nov 14 2007
2Outline
- Old Process
- RD Saga
- Fabrication Procedure
- QC tests
- Fire
- Transmission ratio, after boot/before boot
- Light tightness
- From here to production
- Schedule
3Boots, Old Process
- Problems with Process in May 2007
- Ferrule positioned in mold off polished end, but
the length of the polished end changed causing a
path for the mold material to flow to the front
of the connector. - Material flowed easily, including places we
didnt want, like the polished fiber end the
clips - Material flowed into mold ejection parts, jamming
them up. - In trying to make the boot fire resistant, the
boot would expand and be too wide. - ESH impact of the material, chemical
hood(polyurethane, Al(OH)3 fire retardant) - Remediation
- New mold new mold material
4Mold Redesigned Simplified
Old mold
New mold
5New Mold
- Use sliding clamp to press connector against mold
to prevent mold material from flowing to front of
connector - The Alumilite polyurethane did not flow into
around the connector to the polished fibers as it
was doing with the old mold - No extraction pins which got gummed up in
previous mold - Use straps put in the boot
- Mold cost cut in half
- We have successfully made bootswith new mold and
our originalmolding material, Alumilitepolyureth
ane
6New Boot Mold
Features Simplified reduced cost by
50 Increased draft for easier part removal Mold
cavity is plated polished for easy part
removal No ejector pins or moving plates Modular
design to allow for future changes Added slides
to account for molded connector size
fluctuations Cavity sealing improved to stop
leakage of watery molding materials
7Mold Material The Search
- We research materials for mold
- Worked with PPD ESH on the material
- The requirements are
- Viscosity 1000-15000 cps
- Can be pulled out of mold after 1.5 hours at the
latest - Light tight
- Use mixing nozzle, preferably with prepackaged
cartridges - Durameter A of 90 or harder, RTV doesnt work
here - Fire resistant to UL94
- Like to avoid using a chemical hood for the
molding - After an extensive search, we found nothing which
satisfied all these criteria. - But we have solution which passes the tests
8Hiegl MP5405bk Epoxy the Winner
- Hardens in 15 minutes, this will make production
efficient - Viscosity OK, but it cant be more viscous
- Comes in 50 ml 2 component packages for mixing
gun - No chemical hood needed,
- Probably has the least ESH problems when you
look at the MSDS - Not fire resistant will address later
- Problem, the black material transmits red light
- See the red light from a flash light through a
thick sample, ½ inch thick - Heigl is eager to work with us to satisfy our
criteria - Heigl sent us one 50ml tube of HP5405bk with
additional carbon black - Needed to use a custum modified epoxy
MP5405bk-Mod - Additional carbon black
9Original Material
- The orginal material was Alumilite, but we had
problems - It is more fluid than we want
- We tried to make it less fluid but this didnt
work well - Will require a chemical hood, restricts how we do
production - 4,4 diphenylmethanediisocynate MDI, require ppb vapor
- Not fire resistant
- We tried to make it fire resistant by putting in
ATH - If you put in enough ATH to make it fire
retardant, it expands - If you put in less its worse than if you put in
no ATH. - The ATH makes a gun mixing system difficult to
use - When painted, it did worse than the Heigl.
- Some other materials worked but set in 1.5
hours - One fire retardant material - ESH problems no
mixing system
10Making and Verifying Boots
- We have put boots on 10 cables which have been
tested - In addition, we boots on 4 other cables, in which
we learned we had to add a step to make them
light tight - As of today, 27 cables have boots put on, but
only whats in this talk has been tested. - Verify the cables satisfy the following
requirements - Cables should be fire resistant
- The epoxy should not damage the fibers
- Cables should be light tight
- Note at this point there is no evidence of
physical changes in the epoxy or the epoxy making
physical changes in the boots - Note, if bent, an RTV boot can move a fiber glued
fiber in the connector - We have had Heigl boots for 3 months and boots
still seem OK
11Tasks to Making Light Tight Cables Beyond ODUs
- Have been producing ODUs since beginning of the
year - Cables like ODUs (Optical Decoder Units) only
cables are light tight. - Before gluing fibers in ferrules
- Put on black tube of correct length
- Region from ferrule to black tube was made longer
so that putting on the clip is easy - Insert fiber order is correct in connector
- After gluing
- Put ferrules in gluing fixture and inject Heigl
epoxy into the ferrules to close a hole - Need to do this due to viscous nature of the
epoxy - Can do as many as 40 cables at once
12Tasks to Making Boots Beyond ODUs
- Mold release on mold
- Put ferrule cable in mold
- Inject epoxy into mold, let harden 10 minutes
- Will be doing anywhere between 3-8 cables at once
so this 10 minutes is not a wasted time - Clean up mold release on boot
- File two of the edges so they are not sharp
- 1 coat of fire retardant paint
- Test cable for light tightness
- Test order of fibers with Fiber Order Tester
- Box with multi colored LEDs
13Fire Tests
- Jim Priest suggestion is to paint boots with fire
retardant paint - Old can of black paint
- Sent initial set of Heigl boots painted sample
to for fire test - They ignited at the edges
- These edges were sharp, paint flows off edges?
- Jim suggested getting some new paint and painting
the samples - Filed the sharp edges and painted with green paint
14Fire Tests
- Heigl Orig 1 coat of paint, 3 samples
- Passed, Good Slight ignition and self
extinguished after 1 min of 10 sec applications
of flame - Heigl Orig 2 coats of paint, 2 samples
- Passed, ignition after 45 sec of 10 sec flame
application was able to ignite and burn till he
extinguished - Heigl Carbon 1 coat (2 samples) 2 coats (1
sample) - Good news all the tests went well. They exceeded
the UL 94 V-0 requirement. - Looking at video, 2 samples no flame, one sample
slight flame
15Transmission QC Device
- LED on Calibration Pin Diode and WLS pigtail
- Calibration Pin Diode just in front of LED
- WLS fiber - jumper- cable-jumper-pigtail-pin
diode - Cable Measurement
- Measure without cable
- Direct Measurement
- Transmission (Cable Measurement / Direct
Measurement)
Pin Diodes
LED
Tested Cable
Jumper
Jumper
WLS Pigtail
162d ODU shipment, last 180
- Attenuation length of the clear fiber removed
- 1st transmission
- 2d each channel normalized to 1
- Divided each fiber by cable average
- Cable average
17Fiber average over ODU number
- These are the ODUs which from the previous page
- We QC the prototype cables, but with 5 lengths
the data is more difficult to understand at this
point. Some of the cables were polished at the
very end of a diamond change when were still
trying to understand diamond changes.
18Heigl Effect on fibers, Boot/no Boot
- Measured cables before putting on boot
- Measured after and take the ratio
19After Boot/Before Boot
- Left plot has a damaged jumper for fiber 8, this
makes fiber 8 measurement unreliable - No indication the epoxy is damaging the fibers
20Light Tests
- The Light Leak Checker
- Use R580 -17 (1½ in green extended tube) and
picoammeter - Ped is 0.80 na, HV1200
- Use room light of Lab G, have all lights on
- 2 configurations
- Interchange connectors on box
- The lower connector on box is not completely
light tight for this test - Decided to proceed with light tight test anyway
21Light Tightness
- Current ped
- One cable in this set had a light leak in mold
and this leak was covered - For gain of 106, 0.2na corresponds to about 1
g/ms - Later, test 1 cable
- Shinned bright LED flashlight directly on boot
- Current ped 0.00 na
- Boots appears to be light tight
223 out of 28 problem boots
- 3 of the boots had light leaks, 2 of these boots
were not in the final production technique, but
for these leaks it wouldnt have mattered - 3 problems boots
- Pin hole leak near strap used to pull out cable
- Tape used to plug holes, stuck up slightly
thinning the mold slightly - Air bubble came out of tube while epoxy was
hardening - Problem due to the viscous nature of the epoxy
and the thinning of the boot - Do not want to modify epoxy 3 to 4 month
process - Although, these are easy to touch up we might
tweak the mold - Might make mold 1-1.5 mm thicker
23Tasks to Production
- Finish prototype cable production
- Molds ordered except inserts
- Test insert and order 3 more inserts
- Original mold release didnt work with the new
formulation of Heigl - Switched mold release This one has 2 on health
of MSDS - Although not required by ESH, we will get a hood
to spray the molds with release if we dont find
a new mold release - Possible use of existing spare hood.
- Will try other mold releases to get around this
ESH problem - PAM works well, but we have to clean all the oil
off the cables - Fire tests
- Another fire test with new mold release
- Jim Priest want to do a full fire test to
complete burning
24Schedule
- Expect to start tracking prototype cable
production 1st of year - It will go for about 5 months
- Start production cables, we are 2 months of
critical path