Title: The Improvement of ALARA for the Steam Generator Maintenance
1The Improvement of ALARA for the Steam Generator
Maintenance
- Radiation Safety Department
- The 3rd Plant, Ulchin Nuclear Power Site
2CONTENTS
- Background
- Summary
- Review of ALARA
- The main improvements and effects
- Conclusions
3BACKGROUND
ALARA performed focusing on the SG
maintenance during the 2nd overhaul of
Ulchin Unit 5 in 2006. ? the highest occupational
exposure ? the greatest spread of contamination ?
in particular with poor radiation work
environment
4SUMMARY
Flow chart of SG Maintenance
5SUMMARY
- Radiation work dose
- ? work duration 9/11/200610/4/2006 (24 days)
- ? workers 92 persons (932 man-days)
- ? radiation dose
- Individual dose mSv/person
limit average maximum maximum remarks
limit average work dose accumulated dose remarks
16 (20) 0.55 3.61 15.31 worker of ECT
regulatory limits
6SUMMARY
- - Collective dose (man-mSv)
SG maintenance planned real remarks
manway (open/close) 9 6.58 - 2.42
nozzle dam (install/remove) 9 8.86 - 0.14
ECT 38.5 28.02 - 10.48
lancing FOSAR 12 6.25 - 5.75
total 69.5 49.71 - 19.79
ECT maintenance dose was 16.6 of the total
dose for overhaul (298.7 man-mSv/34days)
7REVIEW OF ALARA
- SG cooling method before the year 2006
- ? Tube and chamber cooled and dried by air
blower after reactor coolant water made them
cooled - - Took a long time to reach the proper
temperature (about 30?) - - The maintenance should be performed in the
work environment - with high temperature and humidity to meet the
overhaul - schedule.
- ? The temporary manway cover did not completely
seal the hole of SG manway due to a decrease the
function of the air blower to dry and purify the
contamination and humidified air inside SG tube.
8REVIEW OF ALARA
Radiation protection ? Work planning ? Source
of radiation ? Protection of radiation worker ?
Area contamination control ? Environmental
condition of work place
9THE MAIN IMPROVEMENTS EFFECTS
- Efficient maintenance minimized the radiation
dose by modifying the cooling method of SG - ? Cooling to utilize the heat exchanger of the
SG blow down system - - cooling time about 46 hours
- - outlet temp of cooling water 15?
- ? Installing the manway temporary cover-only to
seal the hole of SG manway (hot leg and cold leg)
- - dimension (dia.) 700 (T) 3 mm
- - air exhaust hole (dia.) 50 (H) 80 mm
- - spray nozzle hole (dia.) 50 (T) 2 mm
- - material SS304
10THE MAIN IMPROVEMENTS EFFECTS
Cooling Flow
11THE MAIN IMPROVEMENTS EFFECTS
The manway temporary cover-only
BEFORE
AFTER
12THE MAIN IMPROVEMENTS EFFECTS
- Results
- ? Optimization of working environment
- - working hours were shorter and the
troubles of ECT - equipment were less than those of the
previous SG - maintenance
- ? Comparison to 2005
items 2005 (the 1st OH) 2006 (the 2nd OH) remarks
work duration 18 days 14 days - 4 days
temperature in chamber about 80? less than 30 ? - 50 ?
replacement of ECT probe 176 ea 117 ea - 59 ea
work dose man-mSv 72.07 49.71 - 22.36
13THE MAIN IMPROVEMENTS EFFECTS
- Reduction of radiation dose and prevention of
contamination - ? Dose rate reduction of work area
- ? shielded the hot spot (manway retainer plate)
with lead blanket - - before shielding 4.0 mSv/hr
- - after shielding 0.9 mSv/hr
- ? put the high radiation waste probe into the
lead shield cask promptly and dispatched the cask
to the temporary stored area. - ? decontaminated quickly when the surface over
the work area was contaminated from the high
contaminations such as the sludge of the waste
ECT equipment probe.
14THE MAIN IMPROVEMENTS EFFECTS
- Prevention of internal and external
contamination - ? worn respirator
- - air supplied respirator for jumper
- - full-face mask for ECT and manway working
- ? should not touch own face and head
- Preventing the spread of contamination
- ? wore the safety shoes for work place-only
- ? kept the step barrier when going in and out
- ? monitored the trend of surface contamination
level and air borne activity - ? used the tools and equipment with proper
packing, and installed the - cable for ECT to the upper side
- ? periodically checked contamination of safety
shoes and exchanged as - necessary
- Decontaminated and cleaned overall area such
as floor, pipes, grating etc in the end of
overhaul
15CONCLUSIONS
- Our plant could successfully achieve the
reduction - in radiation dose as well as raising the
quality of - maintenance by optimizing the work
environment - such as improvement of the SG cooling method,
- and decreasing the dose rate of work area.
- Preventing the spread of contamination through
- absolute analysis for ALARA from the
preparation - to the beginning of SG maintenance.