LITTLETON/ENGLEWOOD DEWATERING FACILITY - PowerPoint PPT Presentation

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LITTLETON/ENGLEWOOD DEWATERING FACILITY

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Conveyance. Cost Containment. Product of a Collaborative Design. New Dewatering Facility ... Capital savings of $400,000 utilizing PC pumps. O & M costs have ... – PowerPoint PPT presentation

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Title: LITTLETON/ENGLEWOOD DEWATERING FACILITY


1
LITTLETON/ENGLEWOODDEWATERING FACILITY
  • I N T R O D U C T I O N

2
Collaborative Design
  • Needs Assessment - Brainstorming
  • Meeting Facilitation

3
Design Guidelines
  • Permit Limitations
  • Safety and Health
  • Odor Control
  • Resource Optimization
  • Project Scope
  • Cost Containment
  • Participation

4
Key Considerations
  • Clean Process Area
  • Centrifuge
  • Sludge Storage
  • Truck Loading
  • Polymer System
  • Conveyance

5
Cost Containment
  • Product of a Collaborative Design

6
New Dewatering Facility
  • Location
  • Centrate Storage Tank, Covered
  • Odor Control
  • Centrifuge Room
  • Modified versus New
  • Room to work

7
Pump Room
  • PC pumps versus Piston type
  • Allowed for Clean operations
  • One pump per Centrifuge
  • Piping (250 psi)
  • Sludge Hoppers - VFDs
  • Drains
  • Centrate Sample Lines

8
Polymer Room
  • Truck loading dock
  • Large Storage
  • Monorail System
  • Big Bag
  • Tempered Water
  • Trench Drains

9
Sludge Storage
  • Silo
  • Capacity
  • Automated

10
Truck Bay
  • Automated Truck Scale
  • Optional Loading
  • Cleaning

11
Centrate Tank
  • Reused existing Aeration Basin
  • Capital saving of 1,000,000
  • Reduced bottleneck
  • Reduce struvite build up
  • Cleaning made easy

12
New Dewatering Facility
  • Capital savings of 1,200,000
  • Modified existing centrifuges
  • Capital savings of 170,000
  • Modified existing polymer system
  • Capital savings of 400,000 utilizing PC pumps
  • O M costs have been reduced by 75,000
    annually. (More to Come)
  • Maintenance has been reduced 5 fold
  • Lower polymer consumption
  • Tempered polymer water-2 solids increase

13
New Dewatering Facility
  • Reduced dewatering shift from 16.5 hours to 9.5
    hours
  • Truck load out from 16 hours to 15 minutes
  • Truck loaded to specification each time
  • Target and maintain consistent solids output
  • Automation from 2 operators at a 16 hour shift,
    to 1 at 9.5 hours
  • Sludge storage capacity
  • Facility provides for very clean operation
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