Title: CENTURY PULP AND PAPER
1 2 CENTURY PULP AND PAPER
LALKUA, NAINITAL
( A BK BIRLA GROUP OF COMPANY ) ISO 9001
2000 AND ISO -14001 CERTIFIED COM PANY
- AN INTEGERATED PULP PAPER UNIT
- 31320 TPA RAYON GRADE UNIT
- 37250 TPA WOOD BASE WRITING PAPER
- 84600 TPA BAGASSE BASE PAPER
-
ECO MARKED BAGASSE PAPER
3CENTURY PULP AND PAPER POWER ARRANGEMENTS
- 6.8 MW TG SET
- 21 MW TG SET
- 7.5 MVA CONTRACT DEMAND FROM
- UPCL
6,10,000 UNITS /DAY
4CENTURY PULP AND PAPER THERMAL ENERGY
ARRANGEMENTS 23 TPH 46 Kg/cm2 FBC C F BOILER
3 NO 25 TPH 46/Kg/ cm2
SPREADER ST CF BOILER 1 NO 50 TPH 62 Kg/ cm2
FBC CF BOILER 2 NO 40 TPH
46Kg/ cm2 CHEM REC BOILER 1
NO 50 TPH 62 Kg/ cm2 CHEM REC BOILER
1 NO
5THERMAL 16.66
POWER 3.95
WATER 17.64
HIGHLIGHTS
KAIZENS 9750
CHLORINE 17.46
CAPACITY UTILIZATION 106
6TOTAL ENERGY CONSUMPTION
2003-04 2004-05
2005-06 ELECTRICAL UNITS ( Lac kwh/yr )
2180.23 2131.99 2147.58 THERMAL ( Heat
Value Mkcal/yr) COAL
651336.7 590789.2 611208 BLACK
LIQUOR 711616.7 657786
701681 PITH 74641.5
147009 138399 TOTAL
1437595 1395584.2 1451288
7- APPROACH FOR ENERGY CONSERVATION
- AWARENESS EDUCATION TRAINING
- CAPACITY UTILIZATION INCREASED
- OPTIMIZATION OF VOLTAGE
- OPTIMIZATION OF FREQUENCY
- OPTIMIZATION OF OPERATING PROCEDURES
- THRUST ON RECYCLE WASTE MINIMIZATION
- FINE TUNING OF PLANTS EQUIPMENTS
- INSTALLATION OF VFDS
- ADOPT ENERGY EFFICIENT LIGHTING
- USE OF EFFICIENT EQUIPMENT
- TECHNOLOGY UPGRADATION
- ASSESSMENT AND MONITORING
-
8 ASSESSMENT MONITORING
- AUDIT CONDUCTED BY CII APRIL2003
- 39 ENERGY SAVING SCHEMES IDENTIFIED
- AUDIT CONDUCTED BY INGERSOLL RAND SEPT 2003
- 8 SCHEMES IDENTIFIED
- AUDIT CONDUCTED BY ECKO PUMPS FOR PAPER
- M/C III VACUUM SYSTEM OCT2004
- 4 SCHEMES IDENTIFIED
- AUDIT CONDUCTED BY DSCL FOR ENERGY COST
- REDUCTION IN FEB 2004 4 SCHEMES
IDENTIFIED - MOTOR EFFICIENCY ASSESSMENT BY VBI SYSTEMS
- PLANT TECHNICAL AUDITS BY INDEPENDENT
- COUNSULTANTS AUG 2004
9ORGANISATIONAL SET UP FOR ENERGY CONSERVATION
PRESIDENT
Vice President (Elect Inst)
Loss Idn Com
TPM
EC Cell
ISO 14001/ ISO 9001/QC
Energy Centeres
Production Depart 3 Members
MR. Shop Floor Power Hou mental
Cross funct System Committee
Chem Rec Overlapping Teams
Coord. Thermal ElectInst
Committees Quality
Electrical Env Water
Circles
Water Store,Purchase Purta
10- ENERGY CONSERVATION CELL
- FUNCTIONS
- COORDINATE STEAM POWER REQUIREMENTS
- STUDY VARIANCE
- IDENTIFY ENERGY CONSERVATION OPPURTUNITIES
- REVIEW ENERGY AUDIT FINDINGS
- STRATEGY
-
- INCREASE AWARENESS
- ACHIEVE MAXIMUM PLANT EFFICIENCY
- INDUCT LATEST TECHNOLOGY
- ENSURE TIME BOUND IMPLEMENTATION
11TPM
A ZERO BASED APPROACH
ENHANCE PLANT EFFICIENCY
12ZERO BASED APPROACH
LOSS FAILURE DEFECT DOUBT ACCIDENT BREAKDOWN
0
13AUTONOMOUS MAINTENANCE( JISHU HOZEN )
MY MACHINE I MAINTAIN
14EDUCATION AND TRAINING
- SKILL DEVELOPMENT TRAINING PROGRAMME
- TPM AWARENESS 118
- TECHNICAL 722
- BEHAVIORAL 99
- FIRE AND SAFETY 209
- ON JOB TRAINING THROUGH
- ONE-POINT-LESSON
SHEET
15TPM RE- DEFINED
TOTAL POSITIVE MIND
TOTAL POSITIVE MIND
TOTAL POSITIVE MIND
16- LOSS IDENTIFICATION COMMITTEE
- HIGHLIGHT PROCESS INEFFICIENCIES
- CHECK LOSSES OF ALKALI,FIBRE,WATER,
- CHEMICAL AND STEAM
- ARRANGE CORRECTIVE MEASURES
-
17- ISO 9001-2000
- CONTINUAL IMPROVEMENT
- WASTE MINIMIZATION
- ISO14001
- CONSERVATION OF RESOURSES
- ADOPTING CLEANER TECHNOLOGIES
- ALTERNATIVE FIBRE RESOURSES
- UTILIZATION OF WASTE LIME MUD
- UTILIZATION OF WASTE PITH
- QUALITY CIRCLE
- 19 CIRCLES OPERATIVE
18RAYON GRADE PULP SPECIFIC POWER CONSUMPTION
kwhr/ T
76
19WOOD BAGASSE PAPER SPECIFIC ENERGY CONSUMPTION
KWHr/TON
46
20RAYON GRADE PULP SPECIFIC STEAM CONSUMPTION
TON/T
1.34 T/T
21WOOD BAGASSE PAPER SPECIFIC POWER CONSUMPTION
TON / TON
1.79 T/T
22ANNUAL SAVING IN POWER UTILISATION WITHOUT
INVESTMENT
S.NO. SCHEMES INVESTEMENTS (Rs IN LACS) SAVINGS (Rs IN LACS)
1. REDUCED TG FREQUENCY 0 76.20
2. OPTIMISE TG VOLTAGE 0 3.62
3. OPTIMISE RGP VOLTAGE 0 2.49
4. PUT OFF 12.5 MVA TR SET 0 3.02
TOTAL TOTAL 0 85.43
23VARIABLE FREQUENCY DRIVES
24- OTHER ELECTRICAL SCHEMES FOLLOWED
- PROVISION OF LOAD TRANSFER FROM GRID TO TG
- WITHOUT INTERRUPTION TO UTILIZE SOURCES
- PREVENT IDLE RUNNING OF EQUIPMENTS BY
- INTERLOCKING OF PUMPS AGITATORS
- EFFECTIVE CONTROLS LIKE ONE PB FOR
- COMPLETE GROUP EQUIPMENTS OF PLANT
- SWITCH OFF EQUIPMENTS THROUGH TIMERS
- DELTA - STAR FOR LIGHTLY LOADED MOTORS
- NEUTRAL COMPENSATORS FOR UNBALANCE LOADS
- LEDS FOR INDICATING LIGHTS
- LOW LOSS HRC FUSES
- USE OF ENERGY SAVERS FOR LIGHTING CIRCUITS
- USE OF PHOTO CELLS FOR STREET LIGHTS
- SPLITTING OF CIRCUITS FOR BETTER CONTROL
25ELECTRICAL ENERGY SAVINGS
2003-04 2004-05
2005-06 NO OF SCHEMES 41
34 100 SAVINGS / ANNUM KWH
(LACS) 78.614 39.72
77.97 Rs ( LACS) 165
83.41 155.94 INVESTMENT
138.56 86.2 33.25 COST OF
ELECTRICITY Rs 2.10
Rs 404 Lacs PA
26- THERMAL ENERGY CONSERVATION SCHEMES
- EFFICIENT MEANS OF HEATING
- EFFICIENT HEAT TRANSFER
- OPTIMIZATION OF BOILERS FOR COMBUSTION,
- FLUE GAS TEMPERATURE,EXCESS AIR
- INCREASED UTILISATION OF PITH
- MINIMIZE THERMAL LOSSES WASTAGES
- THRUST ON WASTE HEAT RECOVERY
27- ENERGY CONSERVATION MEASURES
- IN PROCESS
- CAPACITY MATCHING WITH THE REQUIREMENT
- PREVENT IDLE RUNNING OF EQUIPMENT
- USE OF CONTINUOUS PROCESS INSTEAD OF
- BATCH PROCESS
- REEL TURN UP SYSTEM ON PAPER M/CS
- USE OF HIGHER EFFICIENCY EQUIPMENT
- THRUST ON WASTE HEAT RECOVERY
28THERMAL ENERGY SAVING SCHEMES
2003-04
2004-05 2005-06 NO OF SCHEMES
7 12 12 SAVINGS
PER ANNUM Mkcal
143608 81752.4 222936 (EQ
COAL ) 35902 20438.1
56610 Rs LACS 984.5
440.35 1165.19 INVESTMENT
893.85 529.67
2714.73 COST OF COAL Rs 1850/TON
Rs 2590 lacs PA
29Replaced of 40 W tubes by 36 W. (1000 no)
2003-04
0.66
0.350
0.176
2
Replaced of conventional chokes with energy
efficient chokes (400 no)
2003-04
0.173
1.44
0.346
-
-
-
-
30Installation of Neutral Compensators.
Installation of VFD in Hot water pump 3 Wash
water pump UNBL 4 ST pump B1.4 stock pump
4 5 6 7
Installation of Sonic Soot blower in B4
Recovery of flash Steam from CBD tank of boiler
31(No Transcript)
32(No Transcript)
33(No Transcript)
34(No Transcript)
35Installation of wet Pith Screw press
36(No Transcript)
37(No Transcript)
38Removal of silica from black liquor through
clarifier and prevent chocking of evaporators
resulting in continuous running and better heat
transfer
Replacement of low efficiency motor of old mud
filter vacuum pump.
Elimination of orifice in inlet of Secondary Air
Fan of BHEL Boiler
Increased Biomass utilization by inter connection
of the gas ducting of Boiler no.4 3 to prevent
positive pressure of furnace
Increase Biomass utilization by increasing the
gap of pith screen
39(No Transcript)
40(No Transcript)
41Compressor unloading control changed from single
step to dual step control
- Following improvements done in compressed air
system - Â Â Installation of zero loss drain valves in air
receiver of compressor 15 Â Â Existing HOC air
drier replaced by refrigerated air drier - Installation of 8 no air receivers
Accurate pressure control of compressed air by
the installation of air Managers on demand side
2 no
42(No Transcript)
43Improved Raw material feed, prevent jamming of
conveyor idle running of equipment result in
stoppage of RGP Chippers in one shift with out
affecting production
Reuse of VF2 back water in VF1 sprays in RGP
bleaching
Mixing of Pre hydrolysis PH Liq of RGP WITH black
Liq. And burning in Boilers. Apart from energy
savings the pollution load was also reduced
Organic solid waste collected during periodic
cleaning of PH Liq. Tank burnt in coal fired
Boilers
Conveyor no 11 carrying Pith from Depither to
Pith yard was provided with a diverter to
facilitate direct loading of Trolleys for
transportation to power house. This prevented
expenses for storage stacking of pith. It also
reduced mixing of stones in pith, absence of
stones resulted in removal of screens and higher
Biomass UTILISATION
SUB TOTAL 39.72
20438.1 - - 81752.4
519.79 529.67
44(No Transcript)
45(No Transcript)
46Replacement of low efficiency motors vacuum pump
in wpp p.mill
Vet Dilution Pump
Insulation of steam lines condensate lines( 17
vet locations in WPP P.Mill
47(No Transcript)
48Trf No. 310
Trf No. 311
49- RGP Chipper area
50(No Transcript)
51Recovery Fib. Chest P/P (Bag)
52(No Transcript)
53(No Transcript)
54Talcum Storage Agitator 3A,3B
55(No Transcript)
56(No Transcript)
57TOTAL ENERGY SAVINGS FOR LAST 3 YEARS
2003- 04
2004- 05 2005-06 INVESTMENT (LACS)
893.85 529.67
2714.73 KWH (LACS) 78.16
39.72 77.97 COAL EQ. TONS
35902 20438
56610 Rs LACS 1141.75
519.79 1321.13
Rs2982 Lacs/a
58- INNOVATIVE SCHEMES
- SUBSTITUTION OF FURNACE OIL
- UTILIZATION OF SOLID WASTE
- OPTIMIZATION OF GENERATION
- WEAK BLACK LIQUOR CLARIFIER
- DIVERTER FOR PITH CONVEYOR
59ENERGY THROUGH RFO HIGH COST FUEL
PRODUCER GAS PLANT
RECALCINE
LIME
LIME SLUDGE
60(No Transcript)
61ENERGY THROUGH COAL - LOW COST FUEL
PRODUCER GAS PLANT
RECALCINE
LIME
LIME SLUDGE
INVESTMENT Rs 338.0
LACS SAVINGS IN2003-04 Rs 196.0 LACS
62BAGASSE STORAGE
63DE - WATERING PITH PRESS
CONTINUOUS DIGESTER
WASHING
BAGASSE
WET PITH 80 MOISTURE
64DE - WATERING PITH PRESS
BAGASSE
WASHING
CONTINUOUS DIGESTER
INVESTMENT Rs 348.29 LACS ANNUAL SAVINGS
Rs 134 LACS
DE WATERING PITH PRESS
50 MOISTURE PITH
65(No Transcript)
66OPTIMIZATION OF GENERATION POWER GENERATION
23.5 MW
130.6
70.65
B4
BH EL
B1
B5
B6
A BL
15.0
62
46
PRDS
110.5
68.94
21 MW
6.8MW
PRDS
27.28
PRDS
COND
33.17
80.75
4.7
3.5
3.5
15.8
37.41
2.5
PLANT
10.5
10.5
PLANT
PLANT
PLANT
67OPTIMIZATION OF GENERATION POWER GENERATION
22.0 MW
133.4
50.6
B4
BH EL
B1
B5
B6
A BL
20.27
46
62
PRDS
111.2
68.94
21 MW
6.8MW
PRDS
23
PRDS
COND
33.42
73.43
3.36
3.5
3.5
2.0
14.71
35.52
PLANT
10.5
10.5
PLANT
PLANT
PLANT
68OPTIMIZATION OF GENERATION
- SAVINGS
- FULL EXTRACTION AT 10.5 Kg/cm2 REDUCED
PRDS FLOW - HIGHER STEAM FOR COGEN
IMPROVED EFFICIENCY - REDUCED VENTING OF STEAM
- STOPPED ONE CFB
- DEARATOR STEAM REDUCED
- ONE BOILER FEED PUMP STOPPED
- LOAD ON COOLING TOWER REDUCED
- COAL _at_2700MT/MONTH
Rs 583 LACS - POWER _at_350 KWH
Rs 56 LACS -
- TOTAL
Rs 639 LACS
69WEAK BLACK LIQUOR CLARIFIER
WPP PULP MILL
BAGASSE PULP MILL
RGP PULP MILL
SCALE FORMATION CAPACITY LOSS INEFFICIENT
EVAPORATOR
WEAK BLACK LIQUOR SOLIDS,FRACTIONAL
FIBRES EARTHY SILICEOUS MATERIAL
70WEAK BLACK LIQUOR CLARIFIER
WPP PULP MILL
WPP PULP MILL
INVESTMENT 120 LACS SAVINGS /ANNUM Rs19.29 LACS
RGP PULP MILL
EVAPORATOR
2000 m3 CLARIFIER
71(No Transcript)
72DIVERTOR FOR PITH CONVEYOR
BAGASSE 1200 TONS/DAY
YARD STONES MIXED WITH PITH
65 FIBRE
35 PITH
BOILERS
PITH STORAGE
73DIVERTOR FOR PITH CONVEYOR
INVESTMENT Rs 0.5 LACS SAVINGS Rs 149.5 LACS
BAGASSE 1200 TONS/DAY
65 FIBRE
BOILERS
35 PITH
PITH STORAGE
TRACTOR TROLLY
74(No Transcript)
75- PROJECTS IDENTIFIED UNDER
- CLEAN DEVELOPMENT MECHANISM
- PITH FIRED BOILER
- DEWATERING PITH PRESS
- BURNING OF PH LIQUOR IN BOILERS
APPROX CERS 11000 PA
76- ENVIRONMENTAL BENEFITS
- REDUCTION IN GHG EMISSIONS
- CONSERVATION OF NONRENEWABLE SOURCE COAL
- REDUCTION OF SOXNOX ASSOCIATED WITH
- COMBUSTION OF COAL
- GLOBAL
- REDUCTION OF GHG ( CO2,CH4 )EMISSIONS
- CONSERVATION OF NONRENEWABLE NATURAL
- RESOURSE i.e COAL
77- AWARDS RECOGNITIONS
- SELECTED AS A MODEL UNIT BY CPCB/NPC FOR
- WASTE MINIMIZATION
- AWARDED CERTIFICATE OF APPRECIATION FOR
- ADOPTING CLEANER PRODUCTION TECHNOLOGY
- UNDER UNEP
- ECO MARK FOR BAGASSE BASE PAPER BY BUREAU OF
- INDIAN STANDARDS
- GREENTECH INDO GERMAN AWARD FOR
- ENVIRONMENTAL EXCELLENCE 2002
- BEST ENERGY CONSERVATION AWARD BY INDIAN
- PAPER MANUFACTURERS ASSOCIATION 2003
04 - IDENTIFIED AS ENERGY EFFICIENT UNIT FOR 2003-04
- BY CII
- RECEIVED ENERGY CONSERVATION AWARD FOR
- 2003-04 BY GOI
78FUTURE PLANS
INVEST SAVI
Rs lacs/ annum INSTALLATION OF ROTARY
COMPRESSORS 142.0 39.74 RETROFITTING OF
ROTARY LIME KILN 200
98.5 RETROFITTING OF MUD FILTER
200 58.06 RETROFITTING OF BLOW
HEAT RECOVERY 58.96 38.92 CONDENSATE
RECOVERY FROM WPP DIG 8.25
24 CONDENSATE RECOVERY FROM RGP DIG 6.5
10.35 IMPROVE LP PRESS FOR PM/C III TH BY
OPTIMIZATION OF PRDS TG
NIL INSULATION JOBS
11.0
45.68
79THANKS