Title: Manufacture and Testing of a Large Zirconium Clad Vessel
1Manufacture and Testing of a Large Zirconium Clad
Vessel
David Clift, P.Eng. Production Manager Ellett
Industries September 14, 2005
2Abstract
- Serviceability depends upon the quality of the
clad corrosion liner - Careful application of design details, skilled
trades systematic application of manufacturing
controls and non-destructive examination.
3Zirconium Clad Steel Reactor
3.6m diameter x 6.5m length (11 10 x 21 2
Shells are 22mm (7/8) thick SA516-70 with 3mm
(0.12) nominal, 2.28mm (0.090) minimum,
thickness Zirconium 702 explosion clad liner. The
hot pressed heads are of 37mm (1.5) SA516-70
with a 4.7mm (3/16) nominal thickness of clad
liner
4 Design Details
Separation of Longitudinal Circumferential Welds
Advantages
- Containment of possible breaches
- Efficient gas purging
- Simplified helium testing
5Material Procurement
- Base Metal N.D.E.
- ASME SA 578 Level C
- grid pattern or continuously scanned - grid
pattern is standard - three inspection levels
- A- least , B - moderate, C - most demanding
allows a discontinuity smaller than can be
contained within a 25mm circle - Cladding N.D.E.
- full compliance with ASME Section VIII IX
- production bend tests, PT examination and 100 RT
before bonding - PT after bonding and, in the case of the heads,
after forming. All clad surfaces were visually
examined
6Ultrasonic Examination of Bonding
ASTM B 898 Acceptance Criteria
- Class C is the standard Inspection Class of B
898 - Class B was specified for this project
7Explosive Cladding
- Current Practice
- an interlayer of titanium when zirconium cladding
exceeds 6.4 mm (1/4) nominal thickness - Explosion detonation (booster) locations
- corner, side or center of plates
- an area of ultrasonic non-bond is typically
located under the detonation point - non-bond related to the size of charge
8Vessel Plate Manufacture
- Central explosion detonation points for both
shell and head plates on this unit - thin cladding, thick backing plates
- ASTM B 898 Inspection Class B ultrasonic
inspection (75mm maximum indication size) - Results
- non-bond areas in shell plate were acceptable
- head plate detonation points were removed as
cut-outs for centrally located nozzles
9Plate Surface Defects
- Damaged areas of clustered gouges were noted on
three of the six shell plates - Gouge depth ranged from 1.2mm (0.047) to 2.4mm (
0.094) deep - Gouge size varied less than 13 cm2 (2 in2) in
area - Root cause - rock fall that occurred during
underground explosive blasting
10Repair Plan
- Weld repair
- shallow gouges (lt1.2mm deep) were weld repaired
in conformance with ASTM B 898. - Controls
- customer approval
- carbide burr removal
- qualified weld overlay repair
- PT inspect
- fully documented
11Repair Plan - contd
- Deep gouges
- Individually ported batten style covers
12Vessel Seam Weld Test Sequence
- Carbon steel welds are applied and specified NDE
performed prior to batten strap attachment - UT the cladding bond adjacent to the end of the
longitudinal seam filler strips to find potential
leak paths - Fit weld longitudinal batten strips, silver
braze to isolate and helium bubble test _at_ 1 bar
pressure - Circumferential welds performed in a similar
manner - Confirming PT of all ZR welds per ASME
13Fabrication - Cleanliness
- Tool surfaces to be of alloy, plated or hardened
steel - Rolls brake forming surfaces - confirmed free
of all surface defects contamination - Weld joint design should minimize carbon steel
welding grinding on process surfaces - Zirconium weld zones are mechanically and
chemically cleaned prior to welding
14Final Cleaning
- Contaminated areas abrasively ground
- Acid wash with HF/HNO3
- Ferroxyl test per ASTM A 380
- spray application of the potassium ferricyanide
test solution on suspect areas - reacts with free iron to form a blue indication
15Helium and Hydro Testing
- Helium Mass Spectrometer testing per ASME Section
V, Article 10, Appendix IV was performed before
and after hydro testing - Purging batten strip cavities
- helium from bubble testing conducted up to a
month earlier had to be purged with clean dry
air to eliminate false indications - Test conditions
- 25 of the vessels maximum allowable working
pressure (50 psig) - approx 20 helium concentration
16Test Results
- Results
- All purge vents located behind nozzle liners,
seams and internal batten style patches were
vacuum sniffed - All readings remained at a background or
atmospheric helium concentration - equivalent to
a leak of 5 x 10-6 atm cc/sec
17Additional Research
- Preparation and analysis of a zirconium weld
overlaid coupon to assess built-up metal quality - CS - TI - ZR construction
After welding and step machining
Prepared block ready to weld overlay
18Results
- ZR overlay welding on both the titanium
interlayer and the zirconium cladding, min
thickness .76mm - Test results confirm a composition containing
titanium and zirconium - No detectable iron was present in any of the test
samples - 100 Zr when a 0.76mm thick layer was applied
over a combined thickness of Ti and ZR of 3.05mm.
The actual thickness of the ZR alone in this case
was 1.3mm
19Questions