Title: Entergy Gulf States, Inc. (Texas) Approved
1Entergy Gulf States, Inc.(Texas)Approved
Proposed Transmission Reliability Projects
- Entergy/ETEC Subcommittee Meeting
- The Woodlands, TX
- November 28, 2006
2Recap of 2004-06 EGSI-TX TransmissionWestern
Region Reliability Improvement Plan Phase II
- Scenario
- In 2003, several planning studies indicated the
Western Region has the potential to encounter
voltage stability problems and thermal
overloading under the double contingencies listed
below. - Loss of Lewis Creek Unit 345 kV Line 119
(Crockett-Grimes) - Loss of Lewis Creek Unit 230 kV Line 568
(China-Jacinto) - Loss of both Lewis Creek Units
- Recommended Solution
- Phase II of the Western Region Reliability
Improvement Plan addresses the projected load
growth with the following projects - 500/230 kV Auto (Cypress) COMPLETED
- Construct Line 822 (China-Porter) 230 kV
COMPLETED - Construct 230/138 kV Porter Substation
COMPLETED - Upgrade Line 599 (Amelia-China) 230 kV
COMPLETED - Install 300 MVAr SVC at Porter Substation
COMPLETED - Install series compensation on Line 822
(China-Porter) COMPLETED - Estimated Cost 115 MM
32006 EGSI-TX Approved Transmission Reliability
ProjectsWestern Region Phase II
INSTALLED SERIES CAPACITOR ON LINE 822
INSTALLED 300 MVAr SVC
4Approved 2007 EGSI-TXTransmission Reliability
Projects inEntergys Construction Plan
Project Name In Service Year Estimated Cost (MM) Comments
Grimes Reconfigure Substation 2007 0.5 Approved
Kolbs Hanks 230 kV Bus Upgrades 2007 0.2 Approved
Splendora Switch Clearance/Replacement (Mandatory Safety) 2007 0.08 Approved
EGSI-TX Underrated Breaker Upgrades (12- 69 kV breakers, Mandatory Safety) 2007 - 2008 1.3 Approved
Calvert Expand cap bank to 12 MVAr 2008 0.6 Approved
Sandy Shores Install 11 MVAr cap bank 2008 0.5 Scoping Only
Porter-Tamina-Conroe Upgrade 138 kV lines 2008 5.5 Approved
Beaumont 69 kV Improvement Plan 2009 8 Approved
Western Region Reliability Improvement Plan Phase 3 2010 2 Scoping Engineering Only
5Approved EGSI-TX Transmission Reliability
Projects in Entergys Construction Plan
- Others
- WRRIP- Phase 3 Scoping Engineering
- Upgrades of underrated breakers (various
locations, mandatory-safety) - Splendora Replace switch (mandatory-safety)
Grimes Reconfigure 345/138 kV Substation
Calvert Expand 69 kV Cap Bank
Calvert
Grimes
Conroe
Porter
Tamina
Helbig
Amelia
Porter-Tamina-Conroe Upgrade 138kV Lines
Hanks
South Beaumont
Kolbs Hanks Upgrade 230 kV Bus
Kolbs
Sandy Shores
Beaumont 69 kV System Improvement Plan
Sandy Shores Add 69 kV Cap Bank
6Grimes 345/138 kV Substation Reconfiguration
- Scenario
- 345/138 kV autotransformers tied to same node of
345 kV and 138 kV ring busses. - Single contingency loss of either 345/138 kV
autotransformer causes the loss of the parallel
autotransformer. - Recommended Solution
- Install a 345 kV circuit breaker to separate
autotransformers on 345kV ring and reconfigure
station to alternate lines and loads. - Install 138 kV breaker to separate
autotransformers on 138 kV ring. - Estimated Cost 0.5 MM (2007 cost only)
7Grimes 345/138 kV Substation Reconfiguration
2007
RECONFIGURE 345 kV BUS
CROCKETT
345kV
INSTALL 345 kV BREAKER
AUTO 1
FRONTIER
138kV
AUTO 2
INSTALL 138 kV BREAKER
8Hanks Kolbs Upgrade Substation Bus
- Scenario
- Firm load within the Port Arthur area has grown
such that the Hanks and Kolbs substation through
bus overloads under the loss of the Sabine to Mid
County 230 kV line. - Recommended Solution
- Upgrade limiting elements of substation bus at
Hanks Kolbs. - Estimated Cost 0.2 MM
9Hanks Kolbs Upgrade Substation Bus
Kolbs
Hanks
10EGSI-TX Circuit Breaker Upgrades
- Scenario
- Based on asymmetrical fault current analysis,
various circuit breakers have been identified as
underrated. - Recommended Solution
- Replace the identified underrated circuit
breakers with appropriately sized breakers. - 2006
- Cow 69kV 5515, 5510
- Orange 69kV 3165, 3145
- 2007
- Orange 69kV 3365
- South Beaumont 69kV 3700
- Port Neches 138kV 3345
- West End 69kV 22135
- 2008
- Orange 69kV 3370
- Dupont Bulk 69kV 3255, 3260
- Helbig 69kV 5585
11EGSI-TX 69 kV System Voltage Support
- Calvert 69 kV Substation
- Loss of 69 kV Line 159 (Bryan APL Hearne)
causes under-voltages at Calvert 69 kV
Substation. - Expand existing capacitor bank to 12 MVAr
- Approximate Cost 0.6 MM
- Sandy Shores 69kV Substation
- Multiple contingencies cause under-voltages on 69
kV Line 175 Beach Line. - Install 11 MVAr capacitor bank
- Estimated Cost 0.5 MM
12EGSI-TX 69 kV Voltage Support
2007
EXPAND EXISTING CAP BANK
INSTALL 11MVAR CAP BANK
13Porter-Tamina-ConroeUpgrade 138 kV Lines 823
886
- Scenario
- Lines 823 886 are 138 kV tie lines to the
Western Region and the Conroe area specifically. - The loss of 138 kV Line 886 (Oak Ridge Porter)
overloads Lines 823 886 above their thermal
limits. - Recommended Solution
- Upgrade Line 886 (Tamina Conroe) to 531 MVA
capacity replace switches and breaker at Tamina
Substation to increase rating on the
Porter-Tamina line segment. - Estimated Cost 5.5 MM
14Porter-Tamina-ConroeUpgrade 138 kV Lines 823
886
2007
UPGRADE TO 531MVA CAPACITY
1569 kV Beaumont Network Upgrades
- Scenario
- In the 69 kV Beaumont area there exists several
single contingency thermal overloads including - 69 kV Line 581 (Helbig Rosedale)
- 69 kV Line 468 (Elizabeth Gallier)
- 230/69 kV Helbig Autotransformers
- 69 kV Bus Tie Breakers (Helbig Amelia)
- Recommended Solution
- Add line breakers at Yankee Doodle 69 kV
Substation. - Close normally open points at Lincoln and
Crockett 69 kV Substations. - Rebuild 69 kV Line 576 (Lincoln South Beaumont)
69 kV Line 98/190 (Dupont Beaumont South
Beaumont) to 106 MVA capacity. - Approximately 5.5 miles of 69 kV transmission
lines - Estimated Cost 8 MM
1669 kV Beaumont Network Upgrades
2007
CROCKETT
CLOSE N.O. BREAKER
CLOSE N.O. SWITCH
YANKEE DOODLE
L-155
VIRGINIA
LINCOLN
L-458
CARDINAL
ADD LINE BREAKERS
UPGRADE LINE 576
L-458
UPGRADE LINE 190
LAMAR
CDT
NITRO
DUPONT BEAUMONT
SOUTH BEAUMONT BULK
UPGRADE LINE 98
172010
Western Region Reliability Improvement
PlanPhase III and IV
- Western Region Reliability Improvement Plan
(Phases 3 4) - Potentially convert 138 kV Lines 524/824
(Jacinto-Lewis Creek) to 230 kV operation. - Construct a 230 kV transmission line from Cypress
to Jacinto. - Construct a 230 kV transmission line from Porter
to Lewis Creek. - Install static and dynamic VAR support in the
Western Region. - Note This set of projects may be modified
based on further activities and developments
occurring at the Louisiana and Texas Commissions.
18Alternatives to the Western Region Reliability
Improvement Plan
- Projects identified in Phases 3 and 4 of the
WRRIP results in greater reliance on and
strengthening of the transmission corridor
between the Western Region and the Beaumont area. - Because of recent events such as the isolation of
the Western Region from the rest of the Entergy
System, the Company has developed several
alternatives to the projects described above.
These alternatives would strengthen the Western
Regions ties to the west.
19WRRIP Alternative 1
- Enhancement of the reliability at Grimes
Substation in order to reduce the reliance from
the Beaumont area - Upgrades of 138 kV Lines 112 and 485 to
sufficient capacity - Installation of a 345 kV bulk tie between Grimes
and Lewis Creek - This option also requires additional firm local
generation.
20WRRIP Alternative 2
- Enhancement of the reliability of the 345 kV tie
to AEP-West in order to reduce reliance from the
Beaumont area. - Upgrade of 138 kV Line 485 to sufficient capacity
- Installation of a 345 kV switchyard on Line 119
including a 345 kV tie line to Rivtrin Substation - This option also requires additional firm local
generation.
21ALT 2
Construct 345 kV Network Into Rivtrin
Enhance 138kV and 345kV Network at Grimes and
Lewis Creek
Construct/ Enhance 230 kV Network Into Lewis Creek
Current Plan Phases 3 4
ALT 1
22Approved 2007 ETEC-RelatedTransmission
Reliability Projects inEntergys Construction
Plan
Project Name In Service Year Estimated Cost (MM) Comments
JNEC Deweyville - Add breakers cut-in Line 2007 0.4 Approved
SHECO - Menard Substation Upgrades 2007 0.1 Approved
SHECO - Turkey Creek Substation Upgrades 2007 0.1 Approved
23Longer-Term Reliability Target Areas (2011)
Potential thermal overloads under single
contingency conditions
- 230 kV Line 496 (China Sabine)
- For the loss of Line 599 (China Amelia)
- 230 kV Line 194 (Hartburg-Helbig)
- For the loss of the Hartburg-Cypress 500 kV line
- 138 kV Line 88 (Dayton Cheek)
- For the loss of Line 496 (China Sabine)
- 138 kV Line 571 (Jacinto Porter)
- For the loss of Line 822 (China Porter)
- 138 kV Line 150 (Dayton Long John)
- For the loss of Line 579 (Jacinto Cleveland)
- 138 kV Line 561 (Gulfrich Crown Orange)
- For the loss of Line 590 (Gulfrich Ausimont)
- 138 kV Line 582 (Oak Ridge Porter)
- For the loss of Line 886 (Tamina Porter)
- 138 kV Line 86 (Dayton Eastgate)
- For the loss of Line 882 (China Porter)
- 138 kV Line 515 (Sabine Port Neches)
- For the loss of Line 516 (Sabine Port Neches)
- 138 kV Line 516 (Sabine Port Neches)
- For the loss of Line 515 (Sabine Port Neches)
- 138 kV overloads in the Jasper-Newton area
- For the loss of the Hartburg-Cypress 500 kV line
- 138 kV Lines from between Lewis Creek and Dobbin
- For the loss of 138kV sources from either the
Lewis Creek or Grimes end - Could be addressed by the Longmire
reconfiguration project
- Other target areas/ projects
- Depressed voltages in the Lacon Substation area
- WRRIP Phase 4