Title: COMPANY INTRODUCTION
1CASE STUDY
ENERGY CONSERVATION OPPORTUNITIES at A Foundry
at Bhiwadi (Rajasthan)
2COMPANY INTRODUCTION
MANUFACTURING GATE , GLOBE AND FLAP VALVES OF
SIZES 1.5 TO 20 AND TURBINE PARTS SUCH AS
CASING TOP / BOTTOM, HORSE SHOE, ETC. MOC CAST
STEEL / SS ANNUAL PRODUCTION 600 TONNE ANNUAL
ENERGY CONSUMPTION FUEL 48 KL ( LDO HSD AND
FO) ELECTRICITY 9.65 LAKH UINTS SPECIFIC POWER
CONSUMPTION (TONNES / LAKH KWH) 62.17
3STUDIES CARRIED OUT DURING AUDIT
ELECTRICAL INDUCTION FURNACE 500 KG (I
NO) HEAT TREATMENT FURNACE 250 KG (1 NO) MOTORS
10HP AND ABOVE (6 NOS) AIR COMPRESSOR 120 CFM
(2 NOS) ELECTRICITY BILL REVIEW THERMAL HEAT
TREATMENT FURNACE 3.5 TONNE (1 NO) LADDLE PRE
HEATING
4SUGGESTIONS FOR IMPROVEMENT
- ELECTRICAL
- INDUCTION FURNACE
- MOLTEN METAL THAT REMAINS IN THE LADDLE, AFTER
CASTING, SHOULD BE RE-POURED BACK INTO THE
FURNACE WHENEVER POSSIBLE - THE ABOVE PRACTICE CAN SAVE RE-MELTING OF AT
LEAST 80 KG OF IRON PER DAY THIS AMOUNTS TO
ANNUAL SAVING OF RS.49,000/- - INSTALL ENERGY METER EXCLUSIVELY FOR THE FURNACE
AND THE DATA SHALL BE RECORDED IN THE LOG BOOK
FOR EVERY HEAT. BY DOING SO THE ELECTRICAL ENERGY
CONSUMED PER HEAT CAN BE MONITORED FOR REDUCING
IDLE TIME - SEPARATE POWER FACTOR INDICATOR TO BE INSTALLED,
FOR MONITORING OF POWER FACTOR OF THE FURNACE,.
THIS WILL ENABLE TO IMPROVE THE POWER FACTOR - AVERAGE ELECTRICITY CONSUMED PER HEAT IS 240
UNITS (KWH) FOR MELTING 500 KG OF METAL i.e.
0.48 UNITS PER KG
5SUGGESTION FOR IMPROVEMENT
- ELECTRICAL
- THE LOADING OF FURNACE TAKES ABOUT 1 HR AS THE
RAW MATERIAL IS PRIMARILY SCRAP OF UNEVEN
SIZES.THIS TIME CAN BE REDUCED IF IT CAN BE FED
IN FORM OF BUNDLES , ESTIMATED SAVING IN TIME
WILL BE ABOUT 10 RESULTING IN SAVING OF RS 2.45
LAKHS PER ANNUM (BASED ON 8 HEATS A DAY AND 300
WORKING DAYS) - HEAT TREATMENT FURNACE
- THE TEMPERATURE OF THE MATERIAL AFTER QUENCHING
AND NORMALIZATION SHOULD NOT BE ALLOWED TO GO
BELOW 150C SO AS TO MINIMIZE HEATING TIME DURING
TEMPERING IN THE NEXT CYCLE. THIS WILL REDUCE THE
CYCLE TIME AND POWER CONSUMPTION BY 16 KWH PER
DAY RESULTING IN ANNUAL SAVING OF Rs.20,000/-
6SUGGESTION FOR IMPROVEMENT
- ELECTRICAL
- ONLY HALF CAPACITY OF THE FURNACE IS USED DUE TO
LESS QUANTITY OF OIL IN THE QUENCHING TANK. BY
INCREASING THE OIL QTY IN THE QUENCHING TANK FULL
CAPACITY OF THE FURNACE CAN BE UTILIZED THIS WILL
SAVE 45 KWH PER DAY RESULTING IN SAVING OF Rs
57,500/- P.A. - IT WAS FOUND THAT MATERIAL BEING NORMALIZED BY
NATURAL COOLING IS ALSO BEING TEMPERED AT 520C.
AFTER DISCUSSIONS WITH THE TECHNICAL PERSONNEL IT
WAS DECIDED TO DISCONTINUE THIS PRACTICE AS IN
THEIR VIEW TEMPERING IS NOT REQUIRED FOR A
NORMALISED PRODUCT. (THIS PRACTICE WAS WRONGLY
STARTED WITHOUT THE KNOWLEDGE OF HIGHER
MANAGEMENT). THIS WILL SAVE 17 KWH PER BATCH OF
400 KG MATERIAL.
7SUGGESTION FOR IMPROVEMENT
- ELECTRICAL
- MOTORS
- THE PERCENTAGE LOADING OF SHOT BLASTING MOTORS (2
NOS) IS AROUND 17. THE EXISTING 10 HP MOTORS CAN
BE REPLACED BY AVAILABLE 5 HP MOTORS. THIS WILL
IMPROVE EFFICIENCY AND POWER FACTOR OF THE
MOTORS. NOT ONLY SAVING OF AROUND RS 11500 PER
ANNUM CAN BE ACHIEVED BUT ALSO THE MOTORS OF 10
HP AND ITS STAR-DELTA STARTER SWITCH GEAR CAN BE
UTILIZED ELSEWHERE - ALL THE 5 BELTS SHOULD BE PROVIDED ON THE
COUPLING BETWEEN MOTOR AND COMPRESSOR. THE BELTS
USED AS THE POWER TRANSMISSION MECHANISM SHOULD
BE TIGHT. - THE WORKING ENVIRONMENT BEING DUSTY, MOTOR
SHOULD BE CLEANED IN EVERY SHIFT TO INCREASE
THEIR EFFICIENCY
8SUGGESTION FOR IMPROVEMENT
- ELECTRICAL
- AIR COMPRESSOR
- THE CFM OF C-2 WAS FOUND TO BE 74 CFM WHERE AS
THE RATED CFM IS 120(61). OVER HAULING OF THE
COMPRESSOR AND REGULAR SUCTION AIR FILER
CLEANING SHALL IMPROVE IT - THE LEAKAGE IN THE SYSTEM WAS EXTREMELY HIGH. AS
A RESULT OF WHICH THE COMPRESSORS IS NOT GETTING
UNLOADED DURING LEAKAGE TEST FOR 30 MINUTES. THIS
INDICATES 100 LEAKAGE IN THE AIR SYSTEM. DUE TO
LEAKAGE, THE PRESSURE AT THE UTILITY IS NOT
SUFFICIENT AND IT IS REQUIRED TO RUN THE 2ND
COMPRESSOR. HENCE THERE IS A LEAKAGE OF ABOUT 74
CFM AND A POTENTIAL OF SAVING RS 2 LAKH PER ANNUM - WHENEVER COMPRESSOR IS RUN ON NO LOAD, SAVING OF
17 KW IS ACHIEVED. IF LEAKAGES ARE ATTENDED,
RUNNING OF 2ND COMPRESSOR CAN ALSO BE AVOIDED - PREFERABLY FLAT BELTS TO BE USED IN PLACE OF
V-BELTS
9SUGGESTION FOR IMPROVEMENT
- ELECTRICAL
- ELECTRICITY BILL REVIEW
- THE AVERAGE POWER FACTOR OF THE INSTALLATION IS
0.93. THE REBATE STARTS FROM 0.95 AND ABOVE.
THERE IS A POTENTIAL SAVING OF Rs 2 LAKH PER
ANNUM BY MONITORING P.F. OF FURNACE AND
ACCORDINGLY INSTALLING SUFFICIENT CAPACITOR BANK - IMPROVEMENT IN POWER FACTOR SHALL REDUCE CURRENT
REQUIREMENT AND CONSEQUENTLY THE MAXIMUM DEMAND
SHALL REDUCE WHICH WILL REDUCE THE FIXED CHARGES
(_at_ 90/KVA) AND THERE IS POTENTIAL OF SAVING RS
26,000 P.A
10SUGGESTION FOR IMPROVEMENT
- THERMAL
- HEAT TREATMENT FURNACE
- FURNACE OIL TEMP AT MAIN STORAGE, PREHEATING TANK
AND BURNER WERE FOUND 38, 45 AND 35C
RESPECTIVELY. THIS WILL RESULTS IN POOR FUEL
AUTOMISATION AND FORMATION OF EXCESS CO IN FLUE
GAS. THIS IS DUE TO ABSENCE OF SERVICE TANK AND
INSUFFICIENT FUEL TEMPERATURE. BY INSTALLING
SERVICE TANK WITH HEATER BETWEEN MAIN STORAGE
TANK AND PREHEATING TANK. TEMPERATURE CAN BE
MAINTAINED AT 45, 80 AND 110 C AT MAIN STORAGE,
SERVICE TANK AND PRE-HEATER TANK RESPECTIVELY AND
ALSO THE ABOVE LINE AND FUEL TANK TO BE PROPERLY
INSULATED - HIGH EXCESS AIR OF 140 WAS MEASURED IN FLUE
GASES DUE TO ABSENCE OF ANY AIR CONTROL MECHANISM
FOR AIR SUPPLY
11SUGGESTION FOR IMPROVEMENT
- THERMAL
- BY REDUCING EXCESS AIR LEVEL FROM 140 TO 30
SAVINGS OF 5 KL OF FURNACE OIL PER ANNUM CAN BE
ACHIEVED. - LADDLE PREHEATING
- PRESENTLY COMPRESSED AIR IS BEING USED AS
COMBUSTIBLE AIR SINCE THE BLOWER IS OF SMALLER
CAPACITY. SO, REPLACEMENT OF EXISTING BLOWER OF
2 HP WITH 5 HP OF 400 CFM AND 40 OF WG WILL
RESULT IN SAVING OF 1.2 KL P.A.