Title: Hygienic and Safe Food Processing Workshop
1- Hygienic and Safe Food Processing Workshop
- CTC Center Lundazi
- May 2007
- Carmen I. Moraru and Catalin Moraru
2- Part I
- Basic Food Hygiene Workshop
- Carmen I. Moraru
3Basic personal hygiene practices during food
processing
- Trainees at the Lundazi COMACO Processing Center
4Practicing proper hand washing
- Demonstration of proper hand washing procedure
using the Germ Glo kit
5Surface cleaning
Station 1
Station 2
Station 4
Station 3
6Checking the efficiency of surface cleaning
7How did we do?
Some did well the first time
some are not there yet!
8To complete the picture dressed for success and
food safety!
Respirator and hard hat for personal protection
necessary when working in the grain handling
facility
- Proper attire for working in a food processing
facility
9- Part II
- Food Processing and Food Product Development
- Carmen Moraru and Catalin Moraru
10The peanut butter process
- Identified issues
- Hygiene standards have improved considerably
since last visit, but still need improvement - Quality problems with the peanut butter
- Phase separation
- Oil leakages
11The peanut butter process in 2005
Roasting
Location dust in the yard
Peanut butter processing
Peanut grading
12The peanut butter process
- Sharing of the processing space with the oil
extraction was a serious contamination source for
the peanut butter
13The peanut butter process - 2007
Peanut processing
14The peanut butter process - Solutions offered -
- Further improvement of hygiene and safety
standards - The workshop offered information and guidance for
improving personal hygiene and safe processing
practices. Key - Proper hand washing
- Proper personnel attire
- Proper cleaning of equipment and
utensils - Pest control
- Some relatively easy to make space design changes
suggested details included in the report
15After training everyone is wearing proper
clothing
To the plant manager
16Preventative safety checks- Pathogen testing of
the peanut butter -
- Qualitative fast tests performed for Salmonella
and E. coli - Negative results for tests performed on May 25,
2007
No color change of the test strips
17Experimental runs for quality improvement of
peanut butter
- Degree of peanut crushing diminished ? coarser
peanut butter expected to minimize oil separation - Suggestions for the emulsification process made
(i.e. use lower temperatures)
- Shelf life study under way to evaluate the effect
of the modified process
18Oil leakage problems
- Phase separation is the main cause for leakages
- Reduced phase separation will also reduce the
leakage problems
- Additionally
- Jar closure not very tight
- Jars not tamper - proof
- Suggested solution
- Aluminum foil discs can be heat-sealed using a
hot clothes iron on top of the jars. Simple and
effective. - Issue current lids will not allow any seal to be
used, due to the ridge that protrudes into jar.
The ridge is meant to provide a good closure, but
not working well.
19Rice processing
Transportation
20Manual grading
21 more grading
22Issues in rice processing
- Large percentage of breakages as a result of
polishing - Economic losses
- Need for solutions for the utilization of broken
rice, other than converting it into rice flour
(which does not have much market potential) - Presence of husks in the finished rice
- Significant manual grading required
- Time consuming and costly
23Evaluation of rice processing operations
- The milling process was evaluated, both
qualitatively and quantitatively - Issues
- Large amounts of broken rice
- Whole kernels found in the broken rice
- Quantitative data included in the report
- Identified cause design flaws of the de-hulling
and polishing equipment
24Solutions offered1. Improvement of rice milling
operations
- Reduction of breakages can be achieved by
- Increasing the gap between the metal rotor and
the metal ridge that caused kernel shearing - Hypothesis tested and validated less breakages
obtained after increasing the gap by 0.5 mm - Further optimization required
- Cleaner rice could be obtained after a low-cost
re-design of the ventilation system of the rice
mill - Equipment design changes suggested
- A drawing of the suggested change was
incorporated in the report
25Solutions offered1. Improvement of rice milling
operations contd.
- More drastic results could be obtained by
reversing the utilization of the two stages of
the rice mills - Use the current polishing stage (lower stage) for
de-hulling. The lower stage abrasive drum will
lead to better de-hulling than the upper rubber
rollers - Use the current de-hulling stage (upper stage)
for polishing. The rubber rollers will not break
the rice and will allow for proper kernel-to
kernel friction required in polishing
Upper stage
Lower stage
- This, combined with the improved ventilation,
could reduce drastically the percentage of broken
rice and will also lead to much cleaner rice - Preliminary testing gave very promising results.
Quantitative data was included in the report.
26Solutions offered2. Processing of value added
products
- Obtaining puffed rice products by extrusion could
be a solution - Challenge current configuration of the extruder
does not allow high temperature high shear
extrusion for puffing applications - Issues to be addressed in the future
- Retrofit the extruder with proper barrel heating
and proper dies, as well as temperature
monitoring capabilities - Technical issues related to adding a new product
line - Define and formulate exactly the product/products
that will be manufactured (product development) - Packaging, storage, and distribution solutions
identified before production starts - Significant extruder cleaning required between
products if multiple products will be
manufactured with the same extruder - Economical questions
- Is there a market for such products?
- Will such a significant undertaking pay off?
27Solutions offered 3. Other suggestions for value
added products
- Easy to make snacks can be made with limited
investment - Issue will only use up small amounts of broken
rice - Products developed during the workshop
(suggestions)
Rice balls (crispy shell, soft core)
Cooked broken rice
Rice candy made out of toasted broken rice and
caramel
Crispy rice chips
28Soy processing
- Soy milk production kicked-off during the
workshop - Some flavored versions developed. Some could
be very successful - Challenges
- Minor equipment troubles
- Water quality
- Proper packaging
- Refrigeration and distribution channels required
29Tofu making
- Tofu made out of soy milk during workshop
- Product liked by a small panel of local people
(CTC employees) - Serving suggestions for incorporation
in local diet provided
30Soy processing by extrusion
- Another possibility
- Meat analogs (or soy bits) could be made if the
extruder is retrofitted with either heating
capabilities or steam injection - Special die required as well
31Soy processing options available with current
equipment
- Soy milk (plain or flavored) and tofu
- Byproducts okara and whey, respectively.
Solutions for byproduct utilization required as
well - Prospects good